| Introduction
In a process plant industry the reliability and effective
availability of equipment are prime requirement to have high
productivity and for rendering faithful service to the consumers.
The reliability of equipment must be ensured, and could probably
be estimated as following:
- By proper equipment selection - 60%
- By proper installation - 15%
- By proper operation and maintenance - 25%
The following case study describes reliability problem with
a LPG handling pump in a field, and the way it was trouble-shooted
and fixed.
History:
These pumps were installed and commissioned in March 1999.
The mechanical seal started to leak intermittently at the
interval of 45-60 seconds. This problem was persisting even
after increasing the RO (restrictive / regulating orifice)
size to 5mm from 3 mm.

Figure 1 Plan 11 (includes the orifice) to
provide the seal flush, and Plan 61 to cool the box. Cooling
water was not provided initially.
Per manufacturer' notes, the estimated pressure in a seal
box is approximately 90% of the discharge pressure, hence
(0.9 x 16) is approximately 14 kg/cm2(g).
Service: LPG
Pump manufacturer: Khimline Pumps, Ltd
Capacity: 76 m3/hr
Rated Head: 173 m
Suction pressure: design = 8 kg/cm2(g); min = 7.0 kg/cm2(g);
max = 10.5 kg/cm2(g)
Operating temperature: 50 deg. C
Vapor pressure: 6.8kg/cm2(g) at operating temperature of 50
deg. C
Sp. Gravity: 0.56
NPSHA: 2.5 m
NPSHR: 1.9 m
Radial bearing: NU-310
Thrust bearings: 7310 back to back

Figure 2 Durametallic (PBR, rotary bellows
seal) mechanical seal, single with viton elastomers. The seal
balance ratio is 70% and pressure gradient factor for the
liquids with low specific gravity is 0.3. The spring pressure
0.45 kg/cm2, per manufacturer notes.
Face combination: Carbon/SiC
The axial hole at the bushing was not present originally (see
discussion later).
Flushing plan: API Plan 11 (3 mm orifice) and provision for
cooling water plan API 61. However, cooling water was not
supplied originally, and connections F/D remained plugged
Observations at site
Seal was leaking intermittently
Suction pressure: 7.5 kg/cm2(g)
Discharge pressure: 16 kg/cm2(g) (steady)
Motor load: 55 amps (steady)
Vibrations: 6.2 mm/sec max
Suspected probable causes of intermittent seal leak:
- hung up rotary head assembly.
- distortion in seal faces.
- axial float in rotor.
- seal chamber pressure below vapor pressure and liquid
flashing into vapor
Observations after dismantling
A) Shining marks observed on carbon face. Rotary face found
good and intact
B) Elastomers found in good condition
C) Both bearings found good and intact. No axial float observed
in the rotor.
D) Impeller found intact.
E) Axial movement of rotary unit found unrestrained and
free of sticky deposits.
F) Seal faces checked for flatness found ok.
G) It was noticed pump impeller has back wear ring but no
balancing hole was provided.
Analysis
- As the rotary head assembly found free on sleeve, item
#1 was ruled out
- Seal faces flatness found within 2 bands - hence item
#2 was ruled out
- No axial float observed in the rotor - item #3 also ruled
out
- The shining marks observed on carbon face revealed that,
there is a loss of lubricating film on the mating faces
which could be due to the formation of vapors in the seal
chamber which were not getting out from the chamber due
to the (too) close clearance in the throat bush. This accumulation
of vapors may be due to the heat generated at mating faces
and dead-ended sealing chamber. The seal chamber bush clearance
appeared to be insufficient to flush out the liquid vaporization
due to heat generated by the seal faces, - especially due
to the fact that cooling water initially was not supplied.
The fact that the seal was failing intermittently with periodic
opening of seal faces and release of LPG in to atmosphere
seems significant. This could be happening because the accumulated
vapors (due to phase change from liquid LPG to gas) would
gradually increase in volume filling out the seal chamber,
and then, when the pressure would build up sufficiently, the
faces would open up, causing vapors release, and the cycle
would repeat.
Applied solution and recommendations
At first, changing to Plan 13 was considered. For LPG / Propane
services, which have a narrow margin between suction pressure
and vapor pressure at operating temperature, seal flushing
Plan 13 was thought to take the excessive built-up vapors
from the sealing chamber back to suction. This plan would
consist of flush line from the seal chamber through R.O. (flow
regulating orifice) to suction. However, it was decided that
this would not solve the problem of vaporization in the seal
chamber, because the seal box pressure would then be even
lower then with using Plan 11, and thus even less margin between
the box pressure and vapor pressure. Thus Plan 13 idea was
rejected.
The history of attempted modifications:
Step 1 Since the in LPG service (seal chamber pressure,
and the heat generated by the rotating seal faces is so close
to vapor pressure) it is important to dissipate the heat generated
at seal faces to avoid rapid vapor formation at seal area.
Initially it was assumed that this was due to vaporization
inside seal box. The orifice size was increased to increase
seal box pressure. Unfortunately, this did not solve the problem.
Step 2 The API 610 8th Edition cooling water Plan 61specifies
the "tapped connection for purchasers use. Typically used
when the purchaser provides fluid (steam, gas, water etc)
to an auxiliary sealing device".
This was initially not connected, as the location didn't have
cooling water available. This was discussed with manufacturer,
pointing to the fact of the LPG service may be sensitive to
heat generation in the seal chamber. The manufacturer felt,
however, that the pump may not require additional cooling,
and so the provisions for the cooling water availability were
not made. With a problem persisting, this then needed to be
addressed, and cooling water circulation through sealing chamber
jacket was then provided, by hooking up the inlet and outlet
line to distanced headers of the neighboring unit, without
the need to dismantle the pump. Unfortunately, this did not
solve the problem either.
Step 3 A 5 mm hole was drilled in the throat bushing,
at the upper portion of it. At the same time, the impeller
four balancing holes were also added, as it was discovered
upon disassembly and examination that they were missing. This
modification worked, and the pump is now running satisfactorily
without any leak.
The seal box pressure for this type of a pump (after modification
with back wear ring and balancing holes) is suction pressure
+35% of discharge pressure as per manufacture's rule of thumb
for the light hydrocarbons:
8.0 kg/cm2 + 0.35% x 16 kg/cm2=13.6 kg/cm2
(g)
Interestingly, this is almost equal to box pressure before
modification (as used by the "90%-rule" calculation above).
Hence, theoretically, this modification does not change the
seal box pressure substantially. What changes, however, is
the amount of liquid from the discharge connection to the
box, and then through the opened-up bushing. In other words,
the restrictive factor was the bushing clearance and not the
orifice in the Plan 11 piping.
Hence by making the hole in throat bush and adding balancing
holes, the passage for circulation of fluid carrying out frictional
heat, became less restrictive, and solved the problem, without
excessive downtime and cost. From our experience, we feel
that light hydrocarbon service pumps, with narrow margin between
vapor pressure and suction pressure, should be provided with
a 3-5 mm drilled hole in throat bushing at the top portion
to allow the vapors to vent away from the seal chamber. |